高级检索
张杰雄, 杨泳星, 张坚俊. 一起10 kV母线失压事件的分析及整改建议[J]. 农村电气化, 2023, (12): 32-35. DOI: 10.13882/j.cnki.ncdqh.2023.12.009
引用本文: 张杰雄, 杨泳星, 张坚俊. 一起10 kV母线失压事件的分析及整改建议[J]. 农村电气化, 2023, (12): 32-35. DOI: 10.13882/j.cnki.ncdqh.2023.12.009
ZHANG Jiexiong, YANG Yongxing, ZHANG Jianjun. Analysis and Rectification Suggestions of a 10 kV Bus Voltage Loss Event[J]. RURAL ELECTRIFICATION, 2023, (12): 32-35. DOI: 10.13882/j.cnki.ncdqh.2023.12.009
Citation: ZHANG Jiexiong, YANG Yongxing, ZHANG Jianjun. Analysis and Rectification Suggestions of a 10 kV Bus Voltage Loss Event[J]. RURAL ELECTRIFICATION, 2023, (12): 32-35. DOI: 10.13882/j.cnki.ncdqh.2023.12.009

一起10 kV母线失压事件的分析及整改建议

Analysis and Rectification Suggestions of a 10 kV Bus Voltage Loss Event

  • 摘要: 某110 kV变电站两回10 kV线路发生相继接地短路故障,由于零序电流互感器回路故障,线路保护拒动造成越级跳闸,引起10 kV母线失压。在故障未切除情况下,值班人员多次试送电,导致系统连续遭受故障电流、电压冲击,造成事故扩大。通过补充检验和对保护动作信息及录波文件进行分析,找到了事故具体原因,并为避免类似事故提出了一些整改意见。

     

    Abstract: Two 10 kV lines in a 110 kV substation have successively ground short circuit fault. Due to the fault of zero-sequence current transformer circuit, the line protection refused to operate, resulting in over-grade tripping, resulting in the loss of voltage of 10 kV bus. Under the condition that the fault is not removed, the dispatcher tried to power on several times, resulting in the system continuously suffering from fault current and voltage impact, resulting in the expansion of the accident. Through supplementary inspection and analysis of protection action information and oscillograph files, the specific cause of the accident was found, and some rectification suggestions were put forward to avoid similar accidents.

     

/

返回文章
返回