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杜卫仕, 王瑞虎, 胡松华. 一起35 kV母线电压不平衡故障的处置[J]. 农村电气化, 2023, (9): 80-82. DOI: 10.13882/j.cnki.ncdqh.2023.09.019
引用本文: 杜卫仕, 王瑞虎, 胡松华. 一起35 kV母线电压不平衡故障的处置[J]. 农村电气化, 2023, (9): 80-82. DOI: 10.13882/j.cnki.ncdqh.2023.09.019
DU Weishi, WANG Ruihu, HU Songhua. Handling of 35 kV Bus Voltage Unbalance Fault[J]. RURAL ELECTRIFICATION, 2023, (9): 80-82. DOI: 10.13882/j.cnki.ncdqh.2023.09.019
Citation: DU Weishi, WANG Ruihu, HU Songhua. Handling of 35 kV Bus Voltage Unbalance Fault[J]. RURAL ELECTRIFICATION, 2023, (9): 80-82. DOI: 10.13882/j.cnki.ncdqh.2023.09.019

一起35 kV母线电压不平衡故障的处置

Handling of 35 kV Bus Voltage Unbalance Fault

  • 摘要: 2022年6月26日,220 kV某变电站35 kV Ⅰ组母线发生母线电压不平衡事故。调查显示,变压器低压绕组中性点未接地导致变压器电容不平衡,同时35 kV Ⅰ母线C相熔断器熔断,导致母线电压不平衡。文章分析了事故原因并总结现场操作和调度处置办法,提出事故预防措施,供运维人员参考。

     

    Abstract: On June 26, 2022, a bus voltage unbalance incident occurred in the 35 kV I-phase bus of a certain 220 kV substation. Investigation revealed that the neutral point of the transformer's low-voltage winding was not grounded, resulting in capacitive imbalane in the transformer. Additionally, the C-phase fuse of the 35 kV I-phase bus was blown, leading to bus voltage unbalance. This paper analyzes the issues, summarizes the problems in on-site operations and scheduling, and provides recommendations for reference by operation and maintenance personnel.

     

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